Another (unsure) Upshur twin (lots of beginner questions?)

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The cam shaft gear was made today. (from some cold rolled mystery steel) I have a 0.5 module hob, i decided to go with that.
0.5 module gears compared to 0.528 module gears (aka 48 pitch) have little smaller teeth. So I adjusted the counts from 30/60 to 32/64.
That pair would have a center distance of 24 mm which is then 0.18 mm too large.
I try to leave both blanks 0.18 mm smaller in diameter, and keep the tooth depth same. I am hoping I will get away with it.
Thre blanks, one was in the middle, so the burr is very small, one has a burr on the climb cut side and the 3rd one has a little messed up tooth profile. cam shaft gear.jpg

Deviating from the schedule I gave the crank shaft a try.
big plate.JPGI found a big plate hot rolled steel 16 mm thick. I could cut a strip off with the band saw that was roughly the proper length.
drilling 3 centers.JPG
Drilling center spots on both ends, using the toolpost as the workholding, with the center drill in the collet block. For height I made a scribe line, for distance using the digital helper.

Interrupted cutting at low rpm with patience went almost uneventful. (The plan suggested to drill and mill out parts before, but I went with plunging directly) The most irritating thing is that the part becomes "transparent" which requires a lot of attention.
K1600_P1010134.JPG
The burr in the last plunge cut was quite big, but it went away as soon as the diameters of first and second plunge cut matched. I made a block that fitted nicely into each gap.
P1010135.JPG
To keep the corners sharp on the crank I made a left and right hand skinny parting tool. K1600_P1010140.JPG
The first trial was totally annealed, because of insufficient patience and cooling. The second went flying, when I wanted to touch up the front angle.
Number 3 and 4 were better. (0.5 mm wide)
After lot more work, interrupted cutting I have my first single piece crank shaft. Might need some modification later. (is a little bit too long on both ends and no gear mounted yet.
K1600_P1010139.JPG

K1600_P1010138.JPG


Greetings Timo
 
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I made the carburetor body on Monday.

carburetor body.JPG
Throttle and jet took a while, small stuff.
Carburetor body with throttle.JPG

The needle is not done yet. Is that a part that needs to be moved a lot? I could make it from a cap head screw, but it would require a hex key to adjust. Or I have to make the complete thing.

Next up the connecting rod. Took a lot of time and head scratch how to make those. I drilled the threaded holes in the longer part and through holes into the shorter block. The shorter block is a little higher than it needs to be. That allows to find the exact line were the two parts meet with the edge finder.

Lshape.JPG
clamped and cut.JPG

Grrr, after cutting I noticed that I put the stock upside down into the vise, so the threded holes ended up almost outside of the part (not were they should be). So I had to make a new part.
new part after 2nd op.JPG
This time the threaded hole is inside the part not under it. ... 😉

Then I made a sort of a grip fixture to hold the small parts. A shape of the connecting rod with recesses to grap the bosses.
grippfixture.JPG
I thought of gluing the parts in, but how to get them out again, and then I had the idea to make a simple cut with the band saw, so that it can be clamped with the vise. (worked quite well)
rods.JPG
Both sides cut, so most of the "big block" disappeared.
K1600_P1010155.JPG
After test fitting them to the crank.
 
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